New BOV = Massive Overboost!?!?!?!?

Discussion in 'Modifications & DIY how-to' started by crashtke, Oct 1, 2006.

  1. crashtke

    crashtke Member Supporting Member

    Ok so I stuck on the new bov today and now I am seeing massive overboost. I am no longer leaking any boost at all. Spool is 100% quicker withough the old leaky factory bov on there. First run I saw over 22 psi according to the gauge....gauge never showed over 17 before with old leaky bov....Only thing I noticed when I got back is the wastegate tubing was slightly pinched from reinstalling the IC (had to change a clamp) but that has been re-adjusted. Have not logged it yet to see what is going on, but it is kinda scaring me! It felt GREAT, but I am worried about long term effects and would like to get boost back under control. Any thoughts?
     
    Last edited: Oct 1, 2006
  2. crashtke

    crashtke Member Supporting Member

    Ok more background...cobb stage 2 (Dp/UP, high flow cat) tweaked for aem sri only...no other changes to cobbs map yet, stock turbo, aem sri, ssautochrome TMIC, stock pill, stock wastegate hoses and connectors, gfb 50/50. Reason for change, stock bpv was leaking. This was really apparent when I put on the new aem sri. I could hear it leaking boost up to 5-7 psi and leaking even more when I was at peak boost (17 before). So I switched to the GFB 50/50 which I got for half the price of a new stock one ($195 from Subaru). I just installed this and now I get over 22 psi before I back off it. Thoughts so far are to ride again and see if the pinched wastegate hose was causing it, do a reset, vishnu reset it and try again...

    My thought at this time is the computer is trying to shoot as much boost in there as fast as it can because it is still thinking that it is recirculating like before with the leaky bpv. Going to do reset and check again.
     
    Last edited: Oct 1, 2006
  3. crashtke

    crashtke Member Supporting Member

    Reset ECU and still over boosting, but not as high. It goes to just at 21 and holds there for a few rpms then tapers down like the stock map and like cobb stage 2. Moving the hose may have done this too, not sure. Going to do some logs today on the way out of town and just try to stay out of the boost as best I can.
     
  4. nsvwrx

    nsvwrx Active Member

    upload some logs... i wanan see this.
     
  5. miloman

    miloman Retired Admin

    is the stage 2 map supposed to run a bar and plate intercooler? i doubt it... the pressure drop across the stock IC is 3+ psi if i remember correctly... the bar and plate intercoolers have a much lower pressure drop... i think that might be ur problem
     
  6. crashtke

    crashtke Member Supporting Member

    Nope it is stock top mount, but even 3 psi puts it at 18.8, not 22 psi. 4th gear on highway went to over 22 and threw a code...posting logs in a sec.
     
  7. crashtke

    crashtke Member Supporting Member

    Ok can't seem to get it to copy over from ST....I try to highlight it and right click and it won't bring up the normal menu to be able to copy and paste....any idea? Any good easy way to do a photo copy of the screen?
     
    Last edited: Oct 1, 2006
  8. miloman

    miloman Retired Admin

    id expect a different pressure drop at different flow rates
     
  9. moose

    moose Infina Mooooooose!

    There's no way he'd hit 22psi from an IC change, is my opinion. Something's f'd up with his boost control, causing insufficient pressure to reach the wastegate actuator.

    Crash: did you move the hose with the pill in it at all? Is there any chance you reversed the hoses when you moved them around, so that the pill is in the hose on the actuator side rather than compressor side?
     
  10. nsvwrx

    nsvwrx Active Member

    the hose might have conme off all the way causing no pressure to ge tot he WSG
    22 on stock turbo is like.. Uh...
     
  11. crashtke

    crashtke Member Supporting Member

    nope, did not dissconnect any of them, just pushed it over so it was not crimped...if I can't find a way to screen print it or copy it somehow, I will just have to enter it in manually.
     
  12. nsvwrx

    nsvwrx Active Member

    press the print screen button on ur keyboard
    open up mspaint
    press crtl +v
    save it as a JPG. and post it up
     
  13. moose

    moose Infina Mooooooose!

    OK, I still think the problem is in:

    Hose from compressor side being messed up.

    Hose to actuator being messed up.

    Leak/tear in hose to boost controller solenoid.

    Boost controller solenoid not working.

    But please post your wastegate targets, as well as logged wastegate duty cycle and turbo dynamics if you have the ability to log that.
     
  14. moose

    moose Infina Mooooooose!

    Screen prints are better off as GIFs. :) (if Paint allows that)
     
  15. crashtke

    crashtke Member Supporting Member

    Throttle position RPM Relative Pressure
    72 2585 5.66
    60 2929 10.88
    60 2978 12.18
    61 3056 13.92
    64 3135 15.81
    85 3390 21.61
     
  16. crashtke

    crashtke Member Supporting Member

    For some reason I did not have wastegates set to log....will have to go get a new one in a few, will try paint and screen prine.
     
  17. moose

    moose Infina Mooooooose!


    Gonna need a little more than that. :)
     
  18. crashtke

    crashtke Member Supporting Member

    [​IMG]

    There we go, no wastegate, but that is the log of high psi.
     
  19. crashtke

    crashtke Member Supporting Member

    [​IMG]

    Another log...
     
  20. goixiz

    goixiz Active Member

    i would not boost more at 22 psi till its ractified
     
  21. crashtke

    crashtke Member Supporting Member

    Might have to do one more log on the way home with the wastegate included...
     
  22. nsvwrx

    nsvwrx Active Member

    no idea why its going that high in boost gonan need wg

    everything else seems good
     
  23. crashtke

    crashtke Member Supporting Member

    Ok, will also be able to pull wideband info on there...got the LC-1 (in theory) set up to work with ST now and display correctly.
     
  24. moose

    moose Infina Mooooooose!

    Please post a screenshot of your wastegate targets as well as turbo dynamics tables from StreetTuner if you can.
     
  25. jayj713

    jayj713 Member

    so uhh, kinda off topic but, how does it feel? :D
     
  26. moose

    moose Infina Mooooooose!

    I can tell you from personal experience that 22+ psi is one hell of an unexpected kick in the pants.
     
  27. miloman

    miloman Retired Admin

    i second that
     
  28. nsvwrx

    nsvwrx Active Member

    my 19 psi is damn amazing. cant imagine 22.
     
  29. crashtke

    crashtke Member Supporting Member

    It is pretty sick till I got the p0244 code and fuel cut, lol. Even part throttle with the current is just sick, 22 psi with 10.5 afr is really smooth. There really is no drop off....and all this from a stock turbo. I know that they found that the td04 on our cars is a bit better than expected, but still kinda woke me up and took me by surprise the first time. The main thing is I was having to shift gears so quick and really getting up to speed in incredible time!!
     
  30. nsvwrx

    nsvwrx Active Member

    but i doubt its safe.. but hey if you dont see anyhtign wrong with it,, might as well?
     
  31. miloman

    miloman Retired Admin

    if ur holding 22 psi till redline, i'd recommend staying off it if u want your rings to last
     
  32. crashtke

    crashtke Member Supporting Member

    Nah, that little 2.0 is gonna pop! I gotta figure this out. Here is the log with wastegate:

    [​IMG]
     
    Last edited: Oct 1, 2006
  33. nsvwrx

    nsvwrx Active Member

    you have a leak somewhere a pin hole in the lines. replace them?
     
  34. crashtke

    crashtke Member Supporting Member

    leak would lead to wastegate pressure wouldn't it? that would be 7-8 right?
     
  35. nsvwrx

    nsvwrx Active Member

    no, as in the tube with the restirtor pill
    no pressure = no waste gate open.
    = infinite pressure!
     
  36. moose

    moose Infina Mooooooose!

    No, you'd see WG boost (7-8 psi) only if you didn't bleed off ANY air. A leak would keep pressure from reaching the actuator and it'd just boost until something gives.
     
  37. crashtke

    crashtke Member Supporting Member

    guess I can make a call to subaru tomorrow and try to get a replacement that is the exact same and just be easy till then. On a side note my stinking AP is not being recognized now by the map software....it sees it, but it says the serial is not right or something. when it rains it pours!!
     
    Last edited: Oct 1, 2006
  38. goixiz

    goixiz Active Member

    the wastegate is like a boost brake the more it opens the less boost you will get. if no air is goin into the wg actuator then no brake then max boost then BOOM.

    if you notice the line to the WG is T ed (after the poison pill) one branch goes to the solenoid the other goes to wg actuator. Best picture ive seen is on the COBB tuning document look at the configuration and check your setup
     
  39. crashtke

    crashtke Member Supporting Member

    Yup I am familiar, one side goes to the turbo outlet and the other goes to the wastegate...I am going to try to replace both of those and the pill just in case today.
     
  40. crashtke

    crashtke Member Supporting Member

    Well Sog does not have them, has to order em....gonna call around I guess and if not order them.
     
  41. nsvwrx

    nsvwrx Active Member

    makesure you replacd e with a stock pill. SOG has alot of sizes
     
  42. crashtke

    crashtke Member Supporting Member

    Found the problem!!! I guess the way the TMIC was sitting it was pushing down on the wastegate actuator where the hose connects and BROKE the nipple that the hose goes on. Subaru wants me to buy a whole new turbo just to get that part at a price of $700...At this point I am going to try contacting some of the shops around here and see what I can find.

    Edit: SS is going to see what he can dig up, but he says that I might have some serious issues with the turbo in the near future as all this time it has been reving to max, but it was just covered up by the leaky bpv...guess the time for a new turbo is closer at hand than I thought!
     
    Last edited: Oct 2, 2006
  43. moose

    moose Infina Mooooooose!

    D'oh! See if you can find the actuator alone from somebody like deadbolt, I bet they have them or can tell you where to find them. It wasn't the nipple on the compressor side that broke, was it? That could get ugly :(

    (Told ya it was a hardware issue...)

    edit: if you can't find one cheap, here's one... http://ipdusa.com/productscat.aspx?CategoryID=1822&NodeID=5722&RootID=1414
     
    Last edited: Oct 2, 2006
  44. crashtke

    crashtke Member Supporting Member

    Edit above after talking to SS. He is going to see what he can do. It is the nipple on the actuator itself. I need to raise up the TMIC about 1/4 of an inch to make sure it clears.
     
  45. moose

    moose Infina Mooooooose!

    Well, with some luck you might be able to get one off a worn/damaged TD04. :)
     
  46. crashtke

    crashtke Member Supporting Member

    Yup, this may just accelerate my plans for a new turbo...I would hate to throw away $200 for an actuator when that money could go towards a whole new turbo! I mean worst case I can pick up a big 16g from TDDC for $600. Best case I can order a nice shiney new deadbolt budged TD05-18g for $899 or a FPtd05-18g for $875. In the mean time if SS can get me one reasonably, I will go with that for now...new turbo not in this months budget.
     
    Last edited: Oct 2, 2006
  47. crashtke

    crashtke Member Supporting Member

    Well have to go to work in a while...this may sound pretty ghetto, but I am going to JB weld it for now...put a little duck tape on 'er and she ran just fine!! (j/k) no duct tape at this point, but I am gonna try to jb it.
     
  48. crashtke

    crashtke Member Supporting Member

    The infinna boost is now gone:hs: A little Jb weld did the trick. I also stuck a couple washers to space up the TMIC so that the problem would not repeat itself. I am really going to have to get a slightly longer TB-IC hose. Something in a nice silicon I think. The samco hose while nice is just a weee bit short now. Another inch of silicon should work fine, maybe even 3/4 inch longer. SS I appreciate you looking for me, not sure if you found anything, but I got it for now. It is a band aid fix, but it works...regular normal boost now, but it still feels better now that it is not being recirculated...much faster spool.

    Edit: I just have to add what a cool guy SS is. He seems to always have time (even though he is proly busy as hell) to answer stupid questions, help out and talk about stuff. If any of you new guys out there have not met him, take some time and swing by there with a burrito for him. Very cool guy.
     
    Last edited: Oct 2, 2006
  49. nsvwrx

    nsvwrx Active Member

    +1 for ss
     
  50. crashtke

    crashtke Member Supporting Member

    One side note..now tha the wastegate is again doing its thing my spool is much slower according to my logs....the cobb ots stage 2 93 may do this on purpose, not sure, but again taking till 3200 to hit 16 where before when the turbo was free wheeling it was hitting 23 psi by 3200. This tells me it can spool much faster than what it is currently doing.
     

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